History of the Telstra Research Laboratories
The Junction Cable Tester
When I was a Trainee Tech, 1969 onward, the PMG
was deep into its rollout of ARF and ARK crossbar telephone exchanges per the
1960 Community Telephone Plan to provide automatic telephone service to pretty
much anyone who wanted a phone. This meant a huge installation programme of
junction cables interconnecting at the telephone exchanges in a sort of
hierarchical/mesh network. A typical junction cable would have 1200 pairs. Each
time Lines Installers installed a cable, it would have to be tested - this would
tie up a senior tech and two helpers for two to three weeks in an extremely
boring job.
You'd use an MDF "test shoe" connector to connect an oscillator to each pair in
turn, while at the other end, your mate, in telephone contact, would connect a
termination and level measuring set. A third chap would look at the measuring
set meter, calling out the reading each time. All pairs in a 100 pair unit of
the cable had to be checked for crosstalk to all other pairs in the unit. That's
12 x 0.5 x 100 x 99 = 59,400 checks per typical cable. When a cross-talking pair
worse than 69 dB was found, we were supposed to put a shrink plastic sleeve on
the MDF block so that the pair could not be used. After a while, you could
literally fall asleep on the MDF ladder while doing this work. All day long,
every day in exchange MDF rooms, you could hear us going "90, 92, 98, 91, 94,
99, 99, 96, 96, 98, 68, 99, 96, 94, 99, aww shit was that a bad pair back
there?" And we had to do some of it over again.
After doing this on about 5 cables, I decided there HAS to be a better way, and
I'm not doing it any more. Back at the depot I thought out a method using
uniselectors (a sort of stepper motor that could select one out of 25 sets of
contacts - used in English Step-By-Step exchanges) pulsed with power transistors
interfaced to the meter circuit of a Siemens TM set. A tech volunteered to make
up a special connector that connected to all 25 pairs in an MDF block vertical
at once. He came up with the goods - a real rough hand-made affair made out of
brass shim, string, and leftovers. I built my transistor & uniselector unit, and
we demonstrated to the depot supervisor that it worked - and all you had to do
was connect it up, connect to the MDF block, sit back, and watch while it found
all the faulty pairs, in five minutes, eliminating hours of drudgery.
Well, it worked great on the bench. In the field it was not very good. This was
because MDF blocks were designed as solder tag blocks, not as a push-on male
connector. The tags had flux and oxidation on them - you couldn't get a reliable
connection. Back at the depot, the tech pulled apart his hand-made connector
female, and manually punched a ridge on all the contacts with a sharpened up
screwdriver, then re-assembled it. We figured that with a ridge on each contact,
providing a pressure point, the act of pushing it on would cut through/clean the
MDF tag and we'd get a good contact. Back to the exchange - it worked! We got
reliable low resistance connections every time on every pair.
My supposed genius came to the attention of the Divisional Engineer. He was
impressed with the immense manhour savings, but not with the rough handmade
appearance. He decided to send me (still just a trainee tech) to Melbourne to
find out how to do it properly. He temporarily made me a Senior Tech as the
Professional Officers Association had some kind of industrial dispute on - they
were making their point by only "going thru channels" this meant they would not
talk to any tech - only the supervisor.
I arrived at Research Labs and met folk who seemed not to have heard about the
industrial action. Right smartly I found myself surrounded by some Engineers,
other sorts of whizzos, and a metallurgist who was expert on relays, switches
and connectors. The metallurgist said he would design a proper tag/contact,
vastly superior to my mate's "home-made" roughie. He burbled on at length about
alloys, contact resistance, tensions, and tolerances. I realised that he was
proposing a flat slide-on contact, and objected, pointing out we had tried that,
and found you need a sharp pressure "knife" to cut thru the flux and oxide
layer. All the TRL guys then ganged up on me, told me I knew nothing, and that I
should leave it to the experts - i.e., them.
I returned to Perth, and after some months, a pair of TRL-built connectors
arrived. They were beautifully made, very neat, with a professional style and
finish way beyond what me and my mate could ever hope to come up with. They had
custom plastic parts and metal work obviously made with precision on a
many-tonne press. They must have cost quite a lot in tooling to make. But they
had flat wiping contacts, not knife-edge oxide-cutting contacts.
We never did get to see if the TRL metallurgist's tags/contacts gave reliable
low resistance connections though. The whole thing could not be fitted onto an
MDF block. Apparently the TRL draftsman had got an MDF block from somewhere and
took measurements off it. It happened that the PMG purchased its' MDF blocks
from three different suppliers, and each made them to slightly different
dimensions - about 3 mm variation top to bottom - as any decent field tech would
know. And each manufacturer had fairly broad tolerances. Didn't matter a bit for
the intended application, having wires hand soldered to them. But the TRL
connector, most elegant as it was, could not be adapted - at best a different
one would be needed for each of the three MDF block types. We stayed with our
own "homemade" connector, as it's flexible design fitted all MDF blocks.
After testing about 20 or 30 junction cables without a hitch, some senior chap
told me I must write it up as an official suggestion and send it to the Staff
Suggestions Board. A year or so later I got back a letter. In it the Board said
that they had in accordance with procedure had my suggestion evaluated by an
appropriately qualified group (TRL). The letter then went on to say that "... my
idea was not of any practical importance, but attached is a cheque for $10 as we
want to reward and encourage young lads with initiative such as yourself." In
fact my idea saved the PMG/Telecom millions. In subsequent years as I
transferred to other postings, as one did, I got called back a couple of times
to repair my uniselector beast.